Ford 6.7L Power Stroke Diesel :: 2011 - Hesitation Or Lag At Takeoff

I'm taking my new to me 2011 KR 6.7 I've had it 1 week, to the dealer tomorrow to get them to look at the hesitation on takeoff. I have read on here that not all trucks are doing it. There is 25500 miles on it and have been averaging 15.3 mpg empty, is this about normal for what people are seeing? I'm running the 3.31 gear ad I thought I would get better mpg. This truck was built in Feb. of 2011 would it have the 400/800 settings or would it have to be flashed?

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Ford 6.0L Power Stroke Diesel :: Power Loss On Takeoff And Then Stopped Now No Start Just Turns Over

So loss power on take off and then stopped at store quick shut it down. Came out of store ten minutes later no start just turns over and over. I replaced IPR last year the one on passenger side near frame if that's correct and perhaps this is the ICP near back of engine?

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Ford 6.0L Power Stroke Diesel :: No Power When Takeoff From A Stop / Black Smoke Blown

So I am not sure exactly what is going on with my truck. It is a 2004 F250 has a 6.0 L. Sometimes when I take off from a stop the truck has no power and blows some black smoke. Then the turbo kicks in and all is fine. It comes and goes when it pleases no matter the temperature. What started happening is when I drive it a steady pace on the highway sometimes the turbo gets quieter and louder and quieter and louder sometimes when it gets quieter I see a little bit of black coming out of the tailpipe. Sometimes it doesn't do it at all. Also sometimes when I let off the gas the truck sounds like it's trying to laugh at me like a wastegate is fluttering.

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Ford 6.7L Power Stroke Diesel :: 2011 - Trans Will Change From Low To 2nd When Takeoff

When i take off in morning truck will change from low to 2nd and hesitate for a second and then go on ok. was sitting at light the other day an went to take off an mashed dn on fuel pedal an it just sit there an then took off, dont no whats going on.:-

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Ford 6.0L Power Stroke Diesel :: Truck A Bit Sluggish At Takeoff - P132B CODE

Can a bad or lazy VGT solenoid cause a P132B code? I just recently had the turbo cleaned and the VGT solenoid replaced about 3 months ago. The truck is a bit sluggish at take off. Is there anyway to check the solenoid to see if its bad?

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Ford 6.0L Power Stroke Diesel :: 2006 - Low Takeoff - Sooty Black Smoke?

06 250 w 65k and it is sluggish on take off, and puffs black smoke most of the time. other than that it runs good.

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Ford 6.0L Power Stroke Diesel :: 2005 F350 - Hesitates / Low Power Driving / Idle

I have a 2005 F-350 Lariat, FX4, CrewCab, with an 8ft Bed if any of that matters. Currently sitting at 191,000 miles and 4,500 Engine Hours I just started running into some issues that I cannot figure out. To start with here is a list of all the mods and prior maintenance that I've done to my truck over that last 6+ years that I've owned it.

I purchased the truck in 2010 and had no issues whatsoever for the first 3 years.....then it all started. While pulling a camper home from vacation "still bone stock" the truck overheated and by the time I realized it it was to late. I ended up blowing a head gasket cracking a head and blowing a hole in my coolant reservoir from the heat & compression of the engine in the coolant system. So to the shop it went.

All of this was done at the same time at just under 4,000 engine hours:

1) Both heads were sent out to be pressure tested "which is where the crack was found", so 1 replacement head and the other trued up and tested by the machine shop
2) All 8 injectors replaced with Airtex/Wells New/Reman
3) ARP Head Studs
4) BPD EGR Cooler
5) New Stock Coolant Reservoir
6) New Stock Oil Cooler
7) Motorcraft Coolant & Oil/Oil Filter Change
8) New Serpentine Belt

After getting the truck back I installed some upgrades that I had wanted but didn't want to do until I had head studs. 4" Turbo back Diamond Eye Performance exhaust, Bully Dog GT Tuner with an EGT Pyro, coolant changed to Caterpillar ELC, Sinister Diesel coolant filtration system, new Optima batteries "I hated them",

Forward a year with no problems I had a crank but no start. I ended up having a bad IPR. A buddy rebuilt the turbo since I had it out and it was leaking. He apparently did something wrong because it took its own life sometime after. So a brand new stock Garrett Turbo with a Wicked Wheel 2 & I changed the IPR "don't remember the brand." Also replaced the factory paper air filter with a cleanable one from AFE that fits in the factory cold air intake.

Little more time and I started to have some overheating issues again, luckily the Bully Dog was monitoring and I had alerts set up so I caught it way before it caused any serious damage. Turned out the fan clutch wasn't working. So I replaced the Water Pump with one from dieselsite.com that has a steel impeller, also replaced the computer controlled fan clutch with a 7.3L mechanical fan clutch and an adapter from BPD.

After that the batteries I hated were replaced. I installed Oddssey Extreme 950CCA ones, a new 185A alternator from FICMRepair.com as well as the complete battery wiring interconnect kit. Did the blue spring upgrade. Replaced my FICM with the BPD 6 phase at 54V setting. Also I changed my starter to an 6.4L Ultima one from O'Reily Auto to bring me up from that slow crank of the 6.0L at about 150RPM to the 225RPM of the 6.4L.

So now on to the current issue. This has happened in the last month and may be related to the issue. I had some small coolant leaks and wanted them fixed. Pressure tested the system & found the radiator and timing cover gasket leaking. I installed a new stock radiator and lower radiator hose. Had the shop do the gasket and a serpentine belt due to cleaners being all over it. During replacement of the timing cover gasket my mechanic found that the LPOP gears had some damage as if something had be in there at one time. Not sever damage just minor. LPOP replaced with brand new one from Ford.

After I got the truck back it was fine for 2 weeks, no leaks or any problems whatsoever. Then I noticed a hesitation as I was leaving work at idle. You could see the RPM's moving up and down by about 50 as it sat there at idle. It got really bad and eventually stalled on me. It fired right back up and ran fine after. I was thinking water in the fuel or just maybe old fuel because it was kinda old and I was at 1/4 of a tank. I went and filled up and it ran great all the way home. Day or so later same thing. At idle you can see the RPM fluctuating and while driving it feels like it has no power at times then it goes away and runs fine. So I changed both fuel filter with Motorcraft ones and put in a new oil filter. It is the Wix brand but I've be running it for years with no issues, one was also in it way before this issues started. The oil has about 2,000 miles on it currently. I verified fuel pressure at idle to be at 70PSI. I tried unplugging the ICP at idle with no change in the hesitation. So I plugged in my SG2 and started to see if I could see anything out of the ordinary.

OAT - 60 Degrees F
KOEO Engine Cold - FMP - 54.5V, ICV - 0.25V, ICP - 0, IPR - 14.9
KOER Engine Warm - FMP - 54.5V, ICV - 0.82V, ICP - 576, IPR - 23.5
Cruise at 40MPH - FMP - 54.5V, ICV - 1.14V, ICP - 965, IPR - 32.9
Cruise at 50MPH - FMP - 54.5V, ICV - 1.42V, ICP - 1,190, IPR - 38.0
Cruise at 60MPH - FMP - 54.5V, ICV - 1.27V, ICP - 1,143, IPR - 37.2

While driving this issue comes and goes very randomly. The only parameter I notice changing alot is the IPR. It jumps around a lot and sometimes it will go to 85. I know that this isn't a good thing so I am going to change the IPR later today or tomorrow. I already had a brand new Motorcraft one to put in, plus at the very least I want to look at the screen. I had read somewhere that there could be air in the oil system and that if you run at a high RPM it can remove this air. I never seen any bubbles or anything on the dipstick. My brother ran the truck for me at 3,000RPM for 5 minutes. No hesitation during the test but he didn't have the SG2 plugged in so I don't know the parameters during the test. I thought that it worked but then it came back after a few miles of driving. The above parameters are from this mornings drive home from work.

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Ford 6.0L Power Stroke Diesel :: 2004 - Surging On Takeoff And Blowing Black Smoke

Ok I have a 2004 f250 6.0L, has 104k on it. A little back story... truck was running well when I started to get surging on takeoff and it was blowing black smoke when it surged. After it hit 1600 rpm it would blow out and run normal. So did some research and found it could be the FCIM, I have the 4 pin and tested it and had 48.5v so it tested good. Did some more research and found symptoms leading towards the ICP so I replaced that and the ICR also.

Upon doing this my surging issue cleared up but now I'm getting a miss around 1200 + rpm weather it's in park Reving it or driving, but it is not throwing any codes, I did check with my code reader. I have also changed both fuel filters and have the EBP sensor on order as I hear they can be troublesome. My question is what should I do next or look at? I was trying to avoid the dealer so I can learn more about the truck in diagnosis.

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Ford 6.0L Power Stroke Diesel :: 2007 - Hesitates At Start Up When Cold?

07 6L gave me a fit the other morning. I spent the night in the mountains Saturday night. Sunday morning was -5. With no place to plug in the block heater. When I started it it bucked and hawed and didn't want to run... It keep surging for a while and finally smoothed out after about 3 mins... Is there an additive that will work for this for the times there is no place to plug in? Oil additive or fuel additive?

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Ford 6.7L Power Stroke Diesel :: 2014 - Hesitates From Dead Stop?

I have a 2014 F250 with the 3.55 rear end and 6500 miles and since new it has a hesitation from a dead stop that I cannot determine if it is normal or not. I took it into a dealer that specializes in diesels and they drove it and told me it is normal. Every time I see someone with the 6.7 I ask them if they have the same problem and I get all kinds of explanations from turbo lag to protecting the tranny. The hesitation I feel is when I throttle from a dead stop. It is a very slight hesitation, but very noticeable, almost like a little "dead spot." If I take my foot off the brake and let it take off on its own for just a second or two and then throttle smoothly it is not there at all. If this is not normal, I want to do everything I can to get it fixed. It is driving me nuts.

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Ford 6.0L Power Stroke Diesel :: 2007 - No Boost - Hesitates While Accelerating?

My truck recently has been giving me the issue of wither having no boost , bogging down as its trying to excelerate , then going into overboost. It idles fine , i have cleaned out the egr . I'm at a complete list on what to do at this point the truck is a 2007 F250 6.0l

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Ford 6.0L Power Stroke Diesel :: 2006 - Hesitates - Hard Start?

I have a 2006 f250 with a 6.0 and I am having some issues with a hesitation and lose of power. The hesitation is worse when under load and other times is not so bad. Also it is non existent at higher RPMs (2500 and up). I changed the egr valve 2 months ago and it seemed to fix the issue (95%) but now it is running bad again. I used Hot Shot oil additive 2,500 miles ago and I changed the fuel filters and changed to 5w 40 Rotella synthetic oil, nothing has changed. I had the FICM changed a year ago with new software updates, still didn't fix it 100%.

Now I am having a "hard" start issue. It takes a bit for the truck to turn over. My batteries are 12 months old and I just replaced the alternator so I am not sure how to proceed.

I did just buy a Scangauge II and I am still figuring out how to use it. It says there is no codes.

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Ford 6.0L Power Stroke Diesel :: Transmission Engages Hard On Reverse / Vibration And Some Knocking Sounds On Takeoff

05 F-350 6L .. Automatic Transmission

When I got the truck I noticed it would slam hard into reverse. Ever since it is taking longer to engage reverse gear and now I have to rev it to 1000 rpms for it to engage with a hard SLAM.

I also noticed that if I do a fast take off, there is a knocking sound coming from drive shaft/differential area (like knock knock knock knock knock then goes away). Then a slight vibration ending at around 30 kph (~20 MPH). There is also some oil leaking from the transmission. I added some mercon sp yesterday - it was a bit low.

My guess for the knocking and vibration is the center support bearings and U-joints. Transmission??? One thing I know I am going to be banging away at that shaft but the transmission problem really scares me.

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Ford 6.0L Power Stroke Diesel :: 2004 - Stumble And Hesitates At Idle / Acceleration?

I have a 2004 f350 6.0 it has 73000 miles on it. I've had the truck for about a month and its developed a slight stumble, hesitation. It does it during idle and acceleration, if I give it more throttle it smooths out. The cel is not on and there are no stored codes.It did this a few days after i bought it,i noticed the map sensor was broke in half so i replaced that and it smoothed out.But it came back. Exhaust is clean no white or black smoke at all.

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Ford 6.0L Power Stroke Diesel :: 2006 - Hesitates Intermittently - Stumble At Idle?

I have a 2006 F-250 4x4 with no cat, and no egr but the valve is still connected. It has about 146,000 miles. Just recently when warm, it has a slight miss every once and a while when stopped and in gear. Just a slight drop in RPM then recovery. Its mainly used on the highway and 99% of the time I set the cruise and its smooth as silk. Every once and a while I feel it stumble once or twice, recover and it is fine for the next 80 miles with no issue. It started as once every few trips but now It seems to be happening at least once every other. I use Motorcraft filters (maybe 6K on the fuel filters) and rotella oil. My scangaugeII shows no codes and no Injector pressure issue (1200-1400 at 75 mph depending on grade) and the FICM voltage stays between 48.5v and 49.0V. What should I check?

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Ford F-150 (2004-2008) :: Code P0175 Cleared Up - Hesitates On Takeoff And Slight Shake Like A Misfire

I have a 2005 F150 5.4 and I recently got a p0175 code. I've replaced the M.A.F. sensor, fuel injectors, fuel filter, new plugs, coils and checked the vac lines but I'm still getting a p0175 code. Ive reset my P.C.M. and the code stopped for 2 weeks but returned later. The truck runs fine when I erase the code but when it returns it hesitates on take off and has a slight shake like a misfire and it makes a bubbly popping sound from the exhaust. Im at a loss of what to do next! Could this be a code stuck in the P.C.M.? My mechanic thinks it may be the cam phasers!

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Ford 7.3L Power Stroke (1999-2003) :: Stalled When Takeoff While At A Stop Sign

The other day while at a stop sign in my e99 F450, I went to take off and stalled. I am not sure if the stall was my fault or not; however, it would not start. I turned the key on and the wait to start light did not come on.

The first thing I checked was the mini 30 amp fuse under the dash that controls the GRP and the fuel bowl heater. The fuse was good, and my heater has been unplugged for a while anyway. Recently my SES light came on with codes that said the glow plugs had low voltage for both banks. I have cleaned the wires a couple times and the light goes out but then comes back on after a minute or so.

I figured that maybe if it was a bad wire it finally went bad so I got jumper cables and started to try and jump wires. I moved them around and found that when I hooked one side to the positive battery terminal and the other to the small key hot wire on the glow plug relay, the light would come on and it would start. I left the cables hooked up and drove the couple miles back home.

After messing with it I figured I could run a new wire. I got a fuse tap, and went from the 30 amp mini fuse that controls this system anyway, and ran it up to the post on the GPR for my new keyed hot wire. The WTS light would cycle and it would crank, but no start. After some more messing around I decided to put both the original wire back onto the post with the new wire that I had just put on; after doing this it started right up. I took it for a test drive and a couple times the engine would act like it stalled, only for a split second. When looking down at the dash immediately after the tach would be at normal RPM and the WTS light would be on, as if I shut the key off and tried to start it again.

I suspect it is the original key hot wire that goes to the GPR. It appears that this wire also has a purpose, other then serving as only a keyed hot wire for the GPR. It has about 6 inches off of the GPR, then it goes into the harness. Where that wire goes? I will just run a new wire instead of having to dig through that harness... that doesn't look like something I would wish upon my worst enemy.

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Ford 7.3L Power Stroke (1999-2003) :: 2001 - Surge Slightly On Takeoff

2001, 7.3 sometimes surges slightly on takeoff ??

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Ford 7.3L Power Stroke (1999-2003) :: 2001 - Hesitates And Won't Go Above Idle Sometimes

I have a 2001 f350 4x4 edge programmer 330k miles. I bought it not running right and thought it would be a easy fix. I'm fairly knowledgeable with the 7.3. Original symptoms where it would run for 5-10 minutes lose power and quit. No restart until it sat for a few hours. P1211 was code, so I figure it's a high pressure oil problem. The truck has a new icp, Ipr, fuel pump, a receipt from dealer where they replaced 1 injectors o ring. I figure the o rings where bad. I replaced all of them.

1 injector was pretty bad the o ring was kinda tore up and disfigured, and 1 had new o rings. Why they would just replace 1 I'll never know. Well the problem still exists, it starts fine sounds good. It will idle 20-30 minutes then get sluggish if I give it any fuel. It's a lot better than before I can floor it and it will rev up and after a few revs it gets better again. If I unplug the icp the idle will go up and down and almost die. Trying to start warm it will just barely run at 4-500 rpm then quit unless I can get it to rev. Once it revs up it seems ok. Does that sound like a hpop problem or am I even on. The right path?

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