Ford 6.7L Power Stroke Diesel :: Upper Radiator Hose Leaking?
After chasing the smell of coolant for a couple weeks, discovered that the upper radiator hose was leaking at the engine. Based on my schedule and drive schedule, and unfamiliar location this last week, I took my truck to the last people I wanted to - the Ford dealer, where they attempted to charge for the hose replacement. During this time I discovered the nature of how these hoses work and asked the tech why they don't just replace the O-rings ... "Ford Motor Company wants to sell you a new hose with labor" - a direct quote from the Ford tech. And that is why Ford is the LAST place I want to go for repairs I cannot perform. I kept the old hose - any spot where you can get the O-rings alone?
View 5 RepliesFord 6.0L Power Stroke Diesel :: Blown Upper Radiator Hose And EOT Temps
This weekend while towing a light load I noticed my FWT and EOT starting to climb rapidly, EOT reached 260 FWT I think about 240. I exited the interstate to find I had a busted radiator hose. I replaced the hose and filled the system with distilled water, but didn't add antifreeze at this time. The system wasn't completely empty.
I noticed once back on the road my EOT seemed to be higher than normal but FWT seemed to be normal. Could the lack of antifreeze cause a greater delta between FWT and EOT? I have seen articles which state do not use Ford Premium Gold Coolant, but to use CAT EL-1 coolant instead. Which should I use?
Ford 7.3L Power Stroke (1999-2003) :: Coolant Flow - No Pressure In Cooling System By Squeezing Upper Hose
Well I was fueling the truck today and I opened to hood to check it out and noticed that there was no pressure in the cooling system by squeezing the upper hose. I did have a spare degas bottle cap and removed the old one slowly and replaced. I have been driving over 30 minutes and it is close to 100 degrees.
I then drove on down the road, the truck is not getting hot. I stopped to look at some running boards and the truck was running and then I came home and still no pressure, the truck is still running, I removed the cap and no pressure, I then removed the small hose going to the top of the degas tank and no coolant came out. I turned the truck off and disconnected the upper hose and some coolant did come out.
Is this normal? The truck runs just fine, just has me worried. I just bought the truck and the previous owner recently replaced the water pump, T-stat, hoses, etc. All parts were bought at O'Reilly. So everything looks good.
Ford 6.0L Power Stroke Diesel :: 2003 F250 - No Start / Lost The Upper Turbo Hose
I have an 03 super duty with the 6.0, came back from vacation with my 5th wheel in tow. Lost the upper turbo hose twice on way home. Managed to get it rigged and made it home and parked it. a week later went to uncouple and move the truck and had some very strange issues. Started fine but could barely make it up driveway (no trailer at this point). No power, felt like when turbo hose came off. Got it moved and checked turbo hose and all was good?? Went out a couple days later and no start.
Checked all relative fuses and relays and all checked good. Jumped starter solenoid and starter worked fine. turned key on and jumped quick connect on right side of engine compartment to battery and it fired right up and ran. Jiggled shifter around in park and neutral and nothing. BTW I always here the relay clicking and swapped with one of the others just to be sure, same thing. After looking on the internet for a day and a half thought maybe a NSS in the tranny but I think I have the 5R110 that does not apply??
Ford 6.7L Power Stroke Diesel :: 2012 - Coolant Leak From Lower Radiator Hose
Just had to replace radiator at 38k on my 2012 SD. Now I have another leak at 41k. Looks like it's wherever the lower radiator hose leads. Kind of a weird junction. I don't think it's coming from above there, but not sure. It's the primary dgas bottle that was low. The radiator was covered under my ESP. We'll have to see what's up with this one. Been eying a denim blue SD at dealer, thinking this is going to talk me out of it though. Not especially happy right now.
View 3 RepliesFord 6.0L Power Stroke Diesel :: Radiator Hose Split While Traveling - 250 Degree EOT After Coolant Loss
Recently I had a radiator hose split while traveling. The EOT got up to 250 degrees before I could pull over and stop the truck. I flushed the cooling system with water, replaced the thermostat, and added Ford Gold coolant as per the recommendations in the Tech folder. My oil temps are higher now than prior to this incident. Unloaded on a flat road my deltas are about 10 to 12 degrees @ 60 mph.
My water temp will stay around 190 to 195 degrees while my EOT have reached 212-215. I pulled a small utility trailer and saw a delta of 17 degrees this was at about 75 mph. Typically unloaded I would only see a delta of about 8 degrees and this was at 80mph. My question is do you think a EOT of 250 would burn the oil, I had Shell Rotella T5 5W40 in the engine. Would it be possible that the oil cooler is partially plugged from this temp?
Passat (B5) :: Upper Radiator Hose Removal?
So i cant figure out how to remove the radiator side of the upper radiator hose. I pulled out the pin but i cant remove the hose.
Do I just pull it straight out? Or do I twist and pull? I dont want to break the connection.
Ford Ranger / B-Series :: 1992 V6 - Upper Radiator Hose Gets Sucked Flat When RPM Is Higher
1992 3.0L V-6 RANGER
New thermostat
New Water Pump
I noticed the other day that the Upper radiator hose gets Sucked Flat when RPM is higher than Idle BAD it completely collapses IDK how it can circulate the coolant very well in this Condition. If the hoses have ever been changed But the Upper hose Really gets sucked flat. I've seen this a few times on vehicles that have been shutdown But they have always expanded upon startup and are fine....
The Lower Looks Fairly Old and only partly collapses under higher RPM.... I am going to change the Upper hose at a Minimum as its really Bad and probably a lot older than I am thinking and really Soft. I am just wondering if the radiator could be plugged up causing some of this.. Or anything else I should check into????
Sonata NF (2006-10) :: Small Leak From Upper Radiator Hose
I smelled antifreeze when walking by my fiances Sonata, so I popped the hood and saw there was a small leak from the upper radiator hose, where it meets the thermostat housing. I adjusted the stock clamp, but the leak was much worse.
I swapped it out for new clamp that you can tighten, and all is well again. But, what I noticed when I had it off was that the metal neck of the housing was really corroded. Only 15,000 on the car, so I was surprised to see that the corrosion on the metal had already built up causing the leak (pushing the hose away from the housing). I scraped and scuffed to get it clean again, but just wanted to give you all the heads up in case you notice a leak in the same area. The antifreeze tested good and is really clean.
Celica :: 1991 Toyota - Water Boiling In Upper Radiator Hose
1991 Toyota Celica 2.2 liter standard water is boiling in upper radiator hose what could be the possible cause of this problem I have changed radiator and cap, water pump, radiator hoses and have flushed the system. could crossed hoses from engine to heater control valve and heater core cause this problem?The head has been checked and no exhaust gas was found in radiator fluid ...
View 4 RepliesFord 7.3L Power Stroke (1999-2003) :: Lower Radiator Hose Replacement
I'm going to be replacing my lower radiator hose so figured might as well switch over to the extended life stuff going to probably go with the Delo ELC.. Supposedly it's good for 750k.
View 14 RepliesFord 6.7L Power Stroke Diesel :: Hesitation / Bucking When Going In The Upper 20s / Lower 30s
Have just about 1,600 miles on tuck born on 12/14/11. Love it, but.. When going slow in subdivision I am getting some hesitation/bucking when going in the upper 20s/lower 30s. When I feel it I look down and I am usually in 3rd. Is this the transmissible thing? When it happened Sunday it felt like it was going to die. If I start off with a quicker start (to get to highway speed) it shifts fine. It just started the last few weekends......
View 14 RepliesFord 6.0L Power Stroke Diesel :: A/C Vents Stuck To The Upper Dash
I recently installed an egr delete and ever since, my vents have been stuck to the upper dash no matter which setting I put on. The vent will push the air conditioning, regular air and heat all the same. I have checked the fuses and they are all good.
View 5 RepliesFord 6.0L Power Stroke Diesel :: 2003 - No Start / Fuel Not Getting Into The Upper Bowl
2003 6.0 no start. turn the key to on and nothing happens. dash lights up as it should but I don't hear the glow plugs cycle and no fuel gets into the upper fuel bowl. turn the key over and nothing happens. No starter click nothing. tried the starter wire to the battery trick and it cranks but does not kick over. checked ficm wires and they are secure as well as the injector wire on the intake manifold. it is the original ficm.
View 6 RepliesFord 6.0L Power Stroke Diesel :: FICM Will Usually Start In Low 30s And Gradually Work Up To Upper 40s
So, I've been having cold start issues for a couple of years now especially when temps get below 25 or so. It started with virtually no issues until temps got into the 20's but got to the point this year where it run a little rough at startup even in the summer. Once ECT gets up around 140* it runs pretty good.
I took it to a diesel shop last year and was told I had 1 bad injector and a bad glow plug. I couldn't afford to do the work, so I waited.
Now after researching this site, I'm more inclined to think it may just be the FICM. I've seen scangauge numbers in the low 20's up to 48.5. On cold morning FCM will usually start in the low 30's and gradually work up to upper 40's. The batteries were both replaced 2 years ago, but I probably should give them a load test. The alternator voltages vary from 11.0 to 12.5 when cold and 12.5 to 14 once warmed up. I have noticed that the AC blower will slow down a little when I sit at a red light, and then pick up again when taking off. I don't notice it with headlights or anything else.
According to Bismarc's spreadsheet, alternator numbers seem to be in the acceptable range, but I don't want to get a new FICM and fry it with a bad alternator. I can get the alternator or the FICM now, but if I need to do both at once I'll need to wait a bit longer.
Ford 6.0L Power Stroke Diesel :: Upper Fuel Bowl Be Empty After Sitting For 30 Minutes?
Should the upper fuel bowl be empty after sitting for 30 minutes?
I believe no. Which would indicate to me a stuck open injector which Iv been suspected of. Iv been trying to track down a miss that I have and Iv been suspicious of a bad injector but ain't been able to pinpoint which one yet.
Ford 6.0L Power Stroke Diesel :: Small Leak On Upper Secondary Fuel Filter
(E350 van)... I smelled diesel fuel inside the van tonight and used my flashlight to investigate the leak. The cover around the blue spring is damp.
Before I remove every again to gain access to the filter housing to fix the leak, what I am may encounter. Seems like a good time to do the blue spring upgrade. Can I access the egr valve to inspect and clean?
What are the possible areas to check for the leak? Sometimes finding little problems leads to finding big problems. When my FICM went out I discovered the battery terminal clamp was broke.
Ford 6.0L Power Stroke Diesel :: Loud Pop As If A Hose Came Off And Power Loss
First there was a loud pop as if a hose came off and a power loss - don't seem to see any hose disconnected. Happened to me once and seemed to return to normal and then happened to my son. Have not driven since the last time. Both times pulling a boat.
Second issue has been going on since I got the truck - bought used apprx. a year ago - believe it to be stock. The time from pushing accelerator until actual kick in is very elongated - sometimes worse than others but very long on the worst side. Usually noticed when needing to pass on the highway. Once kicked in truck runs well.
Ford 6.0L Power Stroke Diesel :: Low Fuel Pressure - Hissing / Air Noise At The Upper Filter Bowl
I have an isspro gauge and did the blue spring about 5 years ago. Since then my fuel pressure is in the 65psi range.
Last week it dropped to 50-55 normal driving and I figured the HFCM was on it's way out (195,000 miles). Replaced the HFCM and the pressure was a bit higher, but not back to it's usual range. Then pulling the boat home from the lake a couple days ago, I saw it at 45psi. On a couple hills it went as low as 40 psi, so I was getting gripped...coasting downhill it only went back up to 50 psi and no higher. Got 'er home and currently not driving it.
In garage with Key On Engine Off, during injector buzz, I can hear a hissing/air noise at the upper filter bowl. Also, the bowl drains empty once the pump cuts off and the sound of air stops too.
I am hoping it's a regulator issue, but I don't know if they are known to wear out or go bad, or if something else in the upper filter housing went bad. So I ordered a new upper fuel filter housing which also has the oil filter tower attached and I'm assuming that these new units would come with the blue spring upgrade already done.
I can check for codes tomorrow when I bring my computer home from work, so I haven't checked for codes yet. I pick up the new filter housing tomorrow and will periodically check back here during the day tomorrow.
Also, while I'm at it: the new HFCM doesn't have the heater. Can I just leave the old connector from the harness un-connected to anything?